3/2006-10/2006

Wow new record for amount of time between updates on the website, sorry about that to anyone that's still reading this, a few of you email me regularly and I appreciate you keeping up. I sold the house in Phoenix and moved back to Texas which I am very happy about, after a 3 month stay with relatives we bought another house so car work can now resume. Since the last entry I have sold the wrong mufflers on ebay and picked up the right ones picked up some exhaust pieces and hung the mufflers and tailpipes, I am still working on the rest of the exhaust as I type this. I acquired some flex joints to be added just off of the turbos and welded those to the reducer flanges but they came out a tad too long so I'll be re routing them another way (pics to come).

I've had a change of heart in my brake upgrades (thankfully this time before I spent very much money) I now plan on staying with the 4 lug setup and plan to just upgrade the rear to disc brakes. I have already acquired the SVO master cylinder and booster as well as a proportioning valve that I'll have to modify but that shouldn't be tough at all. This will allow me to increase the braking power (the 9 inch drum setup is terribly inadequate) and keep the 10 hole wheels that provide the sleeper look with what I think is a fine looking wheel (save your boos and hisses) I'll have to round up a new/used brake pedal since the geometry of the manual brake pedal differs from that of a power brake pedal.

I started the car up with the turbos installed for the first time after it sat in my parent's garage for months while I was house shopping, to my surprise it fired up pretty easily and the whine of the open exhaust turbos sure sounded nice. I found that my Derale fan controller had an open circuit at the fuse so I had to add a different type of fuse holder before the fan would come on. It ran well after its long hiatus and I would have ran it longer if not for the fan not working at the time.

Now that I'm pretty settled again on the living arrangement I can get more done on the car and the updates on this website! Keep an eye out for pics of the latest progress, I'll get them up soon. 

1/2007

Work is still progressing and now that the holidays are out of the way there should be less distractions. On a real high note my car was selected as an editor's choice reader's ride on Fordmuscle.com I was very surprised, I was checking out the new issue and clicked on the link for reader's rides and thought to myself "that would be really neat to get picked for something like this" just as I scrolled down and saw pictures of my car and the write up! So I am very motivated now to make some progress. Since the spot on FM my site has started to see increased traffic so I pried my wallet open and paid the $4 it takes to increase bandwidth transfer so it won't go offline.

Now back to car progress, I did indeed get the fuel pump remounted in its new bracket and  plumbed so it should be ready to be leak tested. It is now closer to the fuel cell and has the fuel filter threaded straight into the inlet for a cleaner look.

 I have also made some strides on the exhaust, the passenger side now runs from the turbo around the engine and down under the car now (all just tacked together to make sure it will work). The driver side looked like it would be easier but the steering shaft had other ideas so I'm still looking at how to get around that without it looking to bad. My ideas of how to route the exhaust has had some changes and alterations along the way but it looks like it is going to match up to the GT tailpipes eventually without much headache.

2/2007-4/2007

Not much done here lately the weather hasn't been cooperating but a few small things have been getting done. While installing  the exhaust I had a clearance issue with the rear brake line and bracket, the tailpipe was rubbing against it. I had some stainless steel 3AN line so I just had to get a few backordered fittings in order to route it around the pipe, this made it a slam dunk. I purchased some 5.0 Mustang muffler brackets to make installing the mufflers a little easier and the bracket for the rear brake line occupied the same area so I ground on the brake bracket so it would fit inside the muffler bracket and I was able to make it all fit.

    Currently I have taken the rear axle out of the car because it has been traded to the 89' GT. The Zephyr's axle had 3.55 gears and they are not optimum for the power band of the twin turbo V8, now that the 89' GT is no longer boosted it can use the extra torque multiplication that the 3.55s offer. In the meantime before the GT's old 8.8 finds its way into the Zephyr it's going to get beefed up at Peyton Performance with welded axle tubes, 31spline axles, an Auburn ECTED, a differential cover/girdle, and rear disc brakes. The 89' GT axle swap was completed today so the next order of business is to take the other 8.8 down to Peyton.

5/2007

I finally got the axle dropped off at Peyton's I ended up making a few changes once the dollar signs started to add up so I axed the ECTED, I hated too but it was clearly the biggest factor in trimming the budget, I ended up going with a full spool but the upside is this allowed me to go with 33 spline axles instead of the 31s I'd be married to had I used the Auburn. Everything else made it through the trimming, I hope to have the assembly back by the end of May if I'm lucky so progress can resume. (its tough to try and do anything else while the rear is up on jack stands) I did manage however to add some Lakewood 50/50 drag shocks in the back while it was up there, now I have Lakewoods all the way around which should help weight transfer enormously. 

 

6-8/2007

OK sorry about the delay on updates, I got the 8.8 back from Peyton's and it looks great, it is now installed in the car, while I was at it I replaced the bushings in the housing and added my adjustable upper control arms as well. Once this was done I have purchased and installed the brake lines and fittings, the brakes are now plumbed entirely with the exception of the Wilwood proportioning valve that is necessary since I went with rear disc brakes, that will be added very soon. I have installed the correct master cylinder and brake booster as well as swapped over to a power brake pedal from the manual one the car had (the geometry is different between the two). I have also purchased an Autometer fuel pressure gauge and I will be finishing that install up shortly as well as adding my Innovate air fuel ratio gauge along with it. I recently acquired (for free) a front and rear sway bar from a 2003 Mustang GT I have added the rear bar and have the front one nearby for street duty when the times comes.

I originally had clearance issues using the ten hole wheels on the rear brakes and I may still get the wheels machined in order to run them but in the meantime I purchased a set of 16 inch 88' Thunderbird turbo coupe wheels which look nice on the car, clear the brakes, and fill up the wheel wells quite adequately. Using the t-bird wheels the front tires were rubbing the coil over setup (if it isn't one thing its another!) to solve this I added some camber adjustment bolts to the struts and moved the wheel out away from the strut, I will later be able to adjust camber using my D&D caster/camber plates so this is not going to be a problem.  

9-10/2007

Wilwood proportioning valve is now installed so the brake system now has all of its hydraulic parts, I have not hooked up the e-brake yet because I am unsure what I need to get it done. I have not had any luck getting a parts list of even a good picture of a Lincoln Versailles e-brake setup so if anyone has this info I'd appreciate seeing it. I also added the 03' Mustang GT rear sway bar which surprisingly took a small amount of grinding to make it fit. I did add my camber bolts to the front struts in order to gain tire clearance as mentioned earlier and it seemed to almost work but I'm sure I'll end up having to run skinnier tires on the front for optimum clearance.

I've still been hard at work on the exhaust but not as much as I should have been but at least things are still moving forward. I'll get some pictures of the downpipes posted since they've been tacked together for a while now and I had to remove them in order to give them the final weld. The fuel pressure gauge install isn't completed yet but then again I haven't been to hard at it to this point.

I forgot to mention I have purchased a pair of weld racing wheels (draglites) off of eBay for the slicks to be mounted on eventually and it was a nightmare getting them shipped to me but they finally arrived and then I ordered lug nuts for them in order to test fit them around the brakes and that shipment got lost and had to be resent! I'm starting to wonder if I was meant to have them?

10/2007-6/2008

No updates on this website in quite a while but I've been getting things done and posted a few pics over on Fordmuscle.com in the "makin' progress" section of their forums. Let me see if I can get things up to date here, the car is now at my place of employment enjoying the convenience of a lift and I have now spent three straight weekends working on it averaging about 8 hours per day on it.

 I ended up replacing the south side lower control arms for some UPR units since they will be a little more forgiving in ride quality and torque box structure.

I had some leaks from the rear brake lines and reran new lines with some different fittings hoping to solve that problem.

 I have added Cody's old Taylor battery box after working out a trade as well as the 0 gauge welding cable and I am still rigging up the master cutoff switch, I think it will turn out great if all goes as planned.

I rerouted my shifter cable and connected it to the side of the transmission which meant I had to hack away part of my trans shield voiding the SFI rating, oh well it will expire due to time before I get the thing down the track anyway it seems!

I have added window felts, beltlines, and runs, dyed the door panels to make things look and sound better.

I added a 3 row Ford motorsport radiator with automatic transmission cooler and I plan on running some nice cooling lines to it asap.

 I just recently rerouted my fuel lines and ran them through the frame in order to gain more room for the exhaust to hang.

 I have acquired a UPR bump steer kit which will go on soon, then I will align the car at work once it is running again.

 The axle is now painted and I added the rear brace kit from LPW racing, it matches and works with the rear differential cover.

That's all I can think of right now but like I said I am back to working on the car with a vengence and I'll be posting up more and more updates and pictures.

 

7/2008-9/2008

Still plugging away at the thing and I've made some real progress I'll go through it list style like the last update.

I ran new transmission lines using some Aeroquip pro flex hose which is a fabric covered high pressure hose that was very easy to work with and looks great.

The charge piping is done and installed/painted!! I also have installed the bypass valves, one of which I was able to use the factory Supra hoses and it lined up perfectly.

The exhaust system is done!! I managed to hang the mufflers and tailpipes on my own and make and install the down pipes, but after tacking the X pipe together I enlisted some help to fit it in, I also added ball and socket connectors to the X for easy removal if I ever need to access the transmission.

I installed the boost gauge and hooked it up directly to the intake manifold.

I completed my master cutoff switch setup and ran it through one of the license plate bolt holes so it can be removed when needed, it works OK but not as good as I had hoped.

The UPR bump steer kit has been installed and I took the time to adjust the steering rack for an even two full turns lock to lock to the left and to the right so everything is centered and ready to be aligned.

I recently bled the brakes and re-tested for leaks and I am down to only one leak so hopefully I can get that handled then I may be ready to fire this thing up.

10/2008

OK things are still rolling along, I've been at it a lot lately and have made good progress.

I seem to have gotten the brake fluid leaks fixed so that's finally out of the way, now I just need to get the e-brake hooked up but that wont prevent a test drive.

I had to diagnose and fix a charging problem that the cutoff switch had caused but I got that handled and the battery now sees over 14 volts. That mark VIII electric fan can waste a battery in no time with no alternator charging, I still feel I could put the car in neutral and turn the fan on in order to back the car up!

The car has been started and has done pretty well considering how long it sat without doing so, I added some fuel cleaner to it when I splashed in five gallons of 93 octane pump and it helped break up any contaminants it seems fine now after a few runs. The car is just as quiet as I had hoped it would be, I was a little nervous about that since I chose my mufflers based on cfm rating but I couldn't be happier with the way it sounds.

I finally got to install the Innovate wideband 02 sensor I've been looking forward to that for a long time, it works great and I can already see it will be a huge help in tuning.  

I found some small fuel leaks and have since repaired them but there are still a couple of oil leaks that will have to wait a while.

It isn't all good news this time after firing the car and warming it up the transmission still doesn't move the car anymore, I'm hoping its just a stuck regulator valve but with my luck the pump went bad and its most likely already lunched the converter and spread the disease to the rest of the trans. I need to check the fluid flow to confirm this but I'll bet the trans will be coming back out before long. At least the car is alive again and this problem is a sign of progress whether good or bad.

11-12/2008

    Well as expected the transmission problem was not something I could have fixed with it in the car so I had to pull it out again. As it turns out it wasn't anything I had done when building it but rather a couple of mismatched parts caused the problem. Since I'm running a late model 5.0 engine it uses a 164 tooth flexplate which requires a big bellhousing equipped C4 transmission but the torque converter I had used was for a small bellhousing so the converter hub to the trans pump wasn't quite long enough to stay engaged.

I also wanted to go ahead and get a working speedometer in the car since the trans was out and couldn't do much more anyway to it so I snagged a new speedo head off eBay and got it installed and I also purchased a new speedo gear, my cable seems to be OK for now. 

After installing the speedometer I was trying to test the instrument lights and realized that my master cutoff switch has stopped working so I'll need to grab another one of those before I can go any further but I now have the transmission reinstalled and the new speedometer head installed and just need to add fluid and fire it up then I'll align it and get ready for a test drive.

1/2009

Well its a new year and I firmly believe this is THE year for the TT Zephyr! Today I managed to finally get around to adding the transmission fluid and tested the trans, it worked! :)  I have now tested all gears and confirmed their operation, this was especially noteworthy as this was my first automatic build, and with the exception of the parts mismatch mentioned earlier I had no problems. On a side note my speedometer work has also paid off as I now have a working speedo, time will tell how accurate it is.  

As far as the master disconnect switch goes I did purchase a replacement, it was a Summit knockoff of a flaming river big switch with lever. I ordered it knowing that the lever that came with it would not be long enough but I figured I'd find a way to make it work. What I didn't foresee was just how easy it would be to make work. I was already using a threaded rod in my own lever design and this lever used a female threaded rod and the two just happen to fit together perfectly! All I had to do was trim the original lever so the handle wouldn't stick out of the back of the car too terribly far and voila! Done.

    I believe I know what caused the failure of the original switch most master disconnects are only rated at maybe 50 continuous amps and my alternator is rated at 130 amps! I had discharged the battery while doing some testing so there's little doubt the battery wanted all the amps it could get and I think this is what lunched the switch. The new switch has me covered as it is rated at 250 continuous amps! I hope to align the car, do a little more tuning and go for a test drive soon.

2-4/2009

Boy how time flies when you're having fun! The Zephyr's first test drive occurred a couple of months ago and it did ok but there are a few small issues to sort out as I knew there would be. If you've been checking out the video section of the website you've already seen a quick spin around the neighborhood where I work, I realize its kind of boring but there are tons of things that need to be accounted for before any "spirited" driving can take place. I did manage to do a couple of mini  burnouts in the parking lot a picture of which can be seen on the latest picture page. In the test drive video the car died as it rolled into the parking lot and I had to fire it up again in order to park it, this turned out to be a misadjusted accelerator pump but adjusting it didn't fix the problem completely so there's still some tuning to be done.

As far as tuning goes, lucky for me I have been using my Innovate Motorsports wideband o2 sensor, this is one of the most helpful tools I've ever used. The version I purchased has the ability to data log up to five different parameters of information to aid in tuning and I'm just getting started with this part of it. I recently acquired and installed a TPS (throttle position sensor) for my Holley carb and a two bar MAP (manifold absolute pressure) sensor as well. RPM is already designed into the data logging cable so I have four others to setup. The TPS will show how much throttle I was giving it at different RPMs and the MAP sensor will data log boost levels.

I'm still currently tying up loose ends in other areas as well, I have bought a pcv valve for a turbo Supra to use so boost won't be able to leak past it when on the gas. I've been having trouble keeping the rear main seal from leaking and I'm hopeful this will aid in that struggle. I also purchased some new carpet but that will have to wait until I can get all the wiring finished and get the floorboards cleaned.

5/2009

OK I now have the sensors installed and setup and I data logged some info today for the first time. the car has now seen a small amount of boost, the first time was while doing a small throttle controlled burnout I was watching the boost gauge like a hawk and saw a measly 1 psi before getting out of it. Today while data logging I hit almost 5 psi and the air fuel ratio was a safe 11.6:1.  As far as seeing the boost earlier today boy I plumbed in stock supra bypass valves and dumped them inside the air filter housings to try and keep noise down from them but wow they got really loud when I let off after hitting just 5 psi in the parking lot!

I got the pcv valve installed with little trouble and also managed to fix the bog off of idle I had, I ended up going up to a #37 accelerator pump nozzle and used a blue pump cam. I want to go for a test drive that is really worthwhile and get some miles on the car, I need to get some insurance on the car so there will be nothing illegal about it while on the road, I did manage to get antique vehicle tags for it so they are good for 5 years, woohoo.

I haven't gotten around to installing the carpet yet (I've been running sensor wires) but it much closer to being done, I bought some cheap foil type insulation to go under it so hopefully it will keep noise down inside the car. If I have enough left over I plan to find a way to add some to the underside of the hood to help out with heat dulling my paint on the hood.

I'm having a lot of fun with the Innovate products, I would recommend them to anyone. In fact I'm thinking about purchasing more of their products the Auxbox has a built in MAP sensor, its own 5 volt reference voltage, and accelerometer (VERY cool), and can data log my exhaust temperature from the type K thermocouple I have in the header. Its very tempting because it has so much already setup and installed within it this may eliminate some wiring I ran (which would be nice) I will be considering this in the future.

6/2009-11/2009

Wow, a lot has happened since May folks. I've gotten divorced, thats how things go sometimes I guess so thats my latest excuse for not doing much on the car. The good part is I didn't lose it and I even got it out and had a little fun with it a month ago. I have a new boost level to report, the data log on the car showed to have hit 12 psi! The excitement was short lived because on that romp I managed to break the transmission and lunched the torque converter, but not to worry I now have a custom built converter made especially for me by Phoenix Transmission Products. I'd recommend them to anyone that is in the market for a domestic based performance transmission at any level. 

I am quite certain that my carburetor will need to be gone through as it seems to be gunked up from sitting too long, among other problems the secondaries were sticking but now that I'm down to one income things will take a little more time to get done but at least most things are done and can continue to move forward.

The new converter has been installed but I still need to get some new bolts as the bolt size and thread pitch have changed. The converter is a really nice piece and you can tell that it was worth the extra money I paid. I hope to test it out very soon.

I hooked up the e-brake cables that were originally intended for the rear brake drum setup, I'll have to test them and see if they work or how well they work.

11/2009-12/2011

Wow new record time for lack of updates, almost two years, at least I managed to post my youtube link on the videos section. Well if you're reading this then you should know that the TTZephyr has been up and running for a while now, the first pass was in October 2010, it didn't run as good as I had hoped but it didn't break so I tried to build and stay positive on that. The videos of the passes are available on www.youtube.com/ttzfer. After that outing in 2010 I packed it in for that year and made some adjustments/improvements, I upgraded the torque boxes and added a new rear suspension from wildrides racecars which included all solid bushing upper and lower control arms as well as solid mounts on the 8.8 axle. This did indeed help as the car finally started to 60ft like I had hoped it would, current best is a 1.58!

So far the car has gone 11.54@114.16 in the 1/4 mile with the stock E7TE heads but I have recently taken delivery of some twisted wedge heads that will hopefully get it in the 10s. I will try to make another picture page dedicated to the new parts, this web editor I'm using isn't as user friendly as what I was using which has been a factor in the lack of updates. stay tuned.


1/2012-6/2013

Ok another long time without any updates but hey thats how it goes sometimes, I got the new heads/intake/rockers installed on the car and fought a few issues initially, it had an exhaust leak because one of the headers is warped, I managed to get it starightened out long enough to install it and get it to seal but if it has to come off again it'll need new headers. I also had to buy new valve covers, trick flows to match the heads I must say they are nice but that was another $120 I didn't expect to have to shell out but they clear the rockers where the grinded stockers wouldn't. After all of that I only managed to test drive the car one time in 2012 due to losing my space at the shop where I am employed to work on it, that was a huge setback and took a long time to overcome. When I drove the car in 2012 it seemed lean under boost and my fan wasn't working without using the manual override, I didn't have the money to do much with it for a while so it sat the whole year. :(


Fast forward to 2013, I managed to recover from my pitfalls and began getting the car going and started tuning on it again, I had to rebuild the carb yet again due to it sitting but it came back to life and I started running it a bit here and there and had my brother in law follow me on a test drive or two and this helped a lot. The issues with my cooling fan working was due to a faulty fan controller but I went with a thermostatic controlled relay from Painless Performance and that solved it. After that I took the car on a 50+ mile drive and really enjoyed being back in the saddle again. there is a video of the short test drive I took with my brother in law in tow and some shenanigans found
here.

Anyway down to business, after getting things working like they should and tuning and tweeking here and there I finally took the car to the track with the new parts on it. I went to the Texas Motorplex and ran new bests, the worst run of the night was an 11.20 which trumps the previous best by over 3.5 tenths. The best run was an 11.10@120.09 best mph on the night was 120.39. So I managed to just miss the 10s but did eclipse the 120mph mark which was an accomplishment. I believe there is still more left in it as I was running pretty rich still even after leaning things out a bit on the jets but until next time check out all the new videos of the runs on my youtube channel.

7/2013-4/2014

Past time for another update, this time there is some good news, the car has finally gotten into the 10s! This was done in November of 2013, it went a 10.98, 10.95, and 10.94 all at over 123mph. I was pretty happy and I know there is still a lot left in it if I can keep the block in one piece. This also marks the first time the car ran 6s in the 1/8 mile with runs of  6.98, 6.95, and 6.95 respectively. Once again I leaned the jets out about 3 more sizes and it is still running pig rich with an average of about 9.9-10.1:1 air fuel ratio, it should be totally safe to run it at 11.5:1 so there should be tons left in it. That being the case I have made a big decision to move to EFI. I have already begun accumulating parts to make the swap and will be running a Megasquirt computer. I hope I can tune it well enough to keep it alive and maximize power but I don't anticipate too much trouble. It will be nice to park it in the garage without the whole thing smelling of fuel after running it. Not to mention total control over fuel and spark timing. Check the youtube channel for videos on the 10 second passes that were made at the Texas Motorplex.

                                                                                       

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