"The Chuckwagon"
84' LTD Station Wagon  page 3

2024
We vowed to return to Hot Rod Drag Week and finish on all 8 cylinders and we did it!


Last year we broke two rocker arm bolts but fixed them not long after getting home, with this done I was ready to go out to a local track and actually have time to test before the event. I had previously tested a couple of months before and found that not only were the brakes not holding on the line but the transmission controller was shifting way too early, even shifting into overdrive during the burnout and the pass!
[Video] Feel free to skip ahead to 1:30 to get right to it.
I contacted US Shift and I tried a few things but in the end, unhooking the rpm signal wire to the controller fixed it, this wire isn't necessary but was an extra I had wanted originally. I had tried to wrap the rpm wire with some shielding but to no avail. Once this was fixed and I knew it wasn't anything I did wrong so I stepped up to their newest controller as mine was a Gen1 version I am now using the remote display Gen3. All is great on this issue now.

OK so we decided we were ready to test again about a month before the event, this time I would be using nitrous. I made 4 passes on the night learning that the brakes still wont hold on the line so I can't really stall it up and give it a good launch, I know this is hurting performance, however it was still fun spraying the thing. I am using a Nitrous Outlet X series kit which is a small 4AN line entry level system, on this night it was jetted for 100hp. There were not many street cars on this night but on my last pass I raced a pretty good running 57 chevy. Here's the video.   I got the win light but at a cost.


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 I had yet another rocker arm bolt break but this time on the driver side, I had vowed when this happened last year on drag week 2023 that I would fix this once and for all and by golly it's time. I got home and swiped the ol plastic and got myself a set of AFR Enforcer aluminum heads with stud mounted rocker arms, I went with the 1.90 intake valve to help with PTV clearance and to not throw the tune off very much.
afrs

I thrashed and got them installed (though I feel the explorer intake is choking things down now a bit) after this I just added 5% fuel to the fuel map above idle everywhere. I also saved some money for the time being and borrowed the Zephyr's rocker arms (I plan to make it up to the Zephyr) Video upon startup and you can tell I'm beat.

I have acquired a small trailer to make things easier to haul stuff around with instead of having to load and unload the wagon everyday. I decided to give it the once over before leaving, good thing I did!
 t1 t2 t3
Found the bearings were in bad shape and one was not turning on the outer race at all. A quick call to etrailer.com and I got new hub assemblies and even added bearing buddies.



The time is here so I got everything loaded up and we took the long trip to Ohio. Below you can see how the hotel actually preferred we park so as not to take up so much room. And the other pic is how the wagon looked while in the tech line.
dwt tl

OK finally to the racing, day 1 National Trail Raceway Hebron, Ohio, we arrive early and our class is the slowest so it runs last except on the last day. My class finally gets the call and I'm up against a really clean Foxbody Mustang GT, foolishly I had a full tank of gas in the car but this would be the most fun race of the week. We leave together my .206 rt to his .209 I jump out on him and the 4R70W is shifting like it owes me money thus keeping the Mustang at bay until we get too about the 1000 ft mark and he slowly overtakes me, my 14.04 to his 13.87.
 Super fun and I ended up catching up with the guy the next day about what a good race it was. After this we pack up and hit the road to Indy...

Day 2 Lucas Oil Raceway Park, Indianapolis, Indiana we arrived uneventfully and waited for our turn, this time I have 1/4 tank but I forgot to remove the spare tire!! arrrgghh!! It still did ok though. Now it was hot on this day so when you are in the car, windows up, A/C off with a race jacket and helmet on you feel like a chicken dinner in the oven at 475° here is the clip of my run but feel free to back up a few MINUTES before this and watch how long I'm stuck sitting there waiting on cleanup in the other lane. When I finally got to run I was sweating badly and pushed the car through the lights thanks to the brake problems I'm having, but it went 13.98 so it was one and done again today. Nothing to do now but head north to Michigan (oh boy was that fun).

Drive to Michigan... 
We were tooling down whatever backroad highway they had us go on via the route map when I just happened to look at the temp gauge, the car had always run perfectly cool up to this point but it was showing 203°. I asked the wife to see if there was an auto parts store nearby, sure enough about 3 miles away off the highway a small town had an O'reilly auto parts. In the past I had noticed the 30 amp fan fuse had gotten a little distorted from being hot, I wrote it off as not being installed very tightly in the fuse block so I added another and bent the terminals opposite each other to hold it tight. Well that was months ago and here we are again and it got more than a little distorted this time.
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 Initially I thought that the fuse was just too hot and melted so I purchased a new fuse block and this time attached the fan wire to a 30amp circuit breaker, this way if it acted up again I could pull over, let things cool down then get on our way. This did work but it would act up whenever we were in stop and go traffic which was only twice I think. After these impromptu repairs we made it to the next checkpoint stop and got our picture to prove we were there but noticed the air shocks were deflated. I pulled off to the side and found that the air line pulled out of the shock when the suspension travelled a little further than it had been doing so I repaired the line then tried to get at least some air in the shocks with a small dinky air compressor I had that plugs into the cigarette lighter. This didn't work but since I left the car running and sitting still the relay tripped and the car got to 223° this was the worst it would get. So for the next 3-4 hours we were investigating and driving to and from every auto parts store in a 10 mile radius. I had discovered the real culprit during this time, 4ish years ago when I wired the fan up it used 8 gauge wires on the factory connector and all I had was 10 gauge I should have doubled up the 10 gauge but I wasn't even sure this fan would work so I wired it up as quickly as possible then was happy when I saw it did indeed work very well. Then like a darn fool I covered up all of the wires with a cheap plastic wire loom which kept me from seeing the high resistance that was causing the problem, (my 8 gauge to 10 gauge wire splices). Only one auto parts store had 8 gauge wire, Advance auto. After I acquired what I needed we found a truck stop (best air compressors for the air shocks) and filled the shocks up and then in a dark truck stop parking lot I rewired my fan. Let me tell you there are some real strange folk hanging out at truck stops at night lol.
dwts
ok so here's how this ended I got things patched up pretty good, left the circuit breaker but had the new 8 gauge wiring we still had to watch the temp like a hawk but this only bothered us in the form of anxiety from here on out. I am currently acquiring parts to fix this properly and take advantage of the pulse width modulation option to keep strain off of the wiring. With this done we were still 100 miles from the second checkpoint at Lane Automotive and another 40 miles from our hotel, we left the truck stop at 11 pm but luck was on our side as the nighttime air was very cool and we motored all the way to Lane automotive and the temp didn't even get hot enough to turn the fan on, it ran anywhere from 176 to as low as 170 while doing 70-75mph down the highway! We arrived at our hotel at roughly 1:30am. This was the worst trouble we would have.

Day3 US 131 Martin Michigan - Got out there early and due to a fog delay we started later than normal but that's ok, got to see friends Eric and Tracy who are about 30 minutes from the track. I would've been so bummed had things gone worse the night before and we hadn't made it. But the ol Chuckwagon may have a future as a good bracket car as you can see here.  One and done and now a bit more worrisome about the fan situation but we had the good fortune of the shortest drive of the week to Milan dragway the next day. On the way Ididit was one of the checkpoints and I got to see another friend Trever who works there and I met his wife as well. I didn't really know if he would be there around 8:30-9:00pm when we got there but he was, our hellos were brief as the place was packed with other racers getting their photos and getting to hotels for the night.

Day 4 Milan dragway - Got a much needed good night's sleep and arrived to another fog delay. Trever showed up and this time we had more time to visit. The bummer thing about this day was the official Hot Rod Drag Week live feed cutoff 2 hours of runtime and that was when I ran but luckily my wife got video! Here it is. 13.99 If only it were a bracket race! Now it's time to get back to National Trail Raceway for the last day!

Day 5 Hebron, Ohio the final day all we have to do is stage, break the beams and we've done it. Is that what I did? Heck no! The truck and trailer are here let's fire up the nitrous! I had stepped down from a 100hp shot to a 75hp shot just to be safe. I plan to get back on the Zephyr if this car makes it home hitting on all 8 (and it did). Here's the nitrous pass and the conclusion of Drag Week 2024 for us. 13.57@103.9

All in all we had a great time and can't wait for next year, I would really like to get the Zephyr to this event or one like it. It would be fun to have a faster car even if it isn't as comfy.


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